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With the engine
completed, it was time to run some tests and find out if
the HR-1 would work as planned. The engine was rolled out
on its test stand and fired up. The engine did manage to
run. Throughout many tests, a few minor problems were noticed
and steps were taken to correct them.

Scroll entrance burned away
This is what
happens when one of these engines overheats. The fuel was
not burning fast enough and carried the immense heat into
the scroll entrance. It was so hot it acted like a torch
and melted the metal away. To fix the inlet, a grinding
stone was used to remove the areas of the cast iron that
had melted. The metal was then smoothed out to attempt to
avoid having a hard edge that could create further hot spots.

Jet nozzle
This nozzle is
the same size as the turbine exit and goes up inside sealing
off at the housing. I did this because the opening of the
turbine scroll is five inches and the turbine wheel is three
and three quarters. The nozzles were made from five-inch
pipe that I added a step on to so the size would be reduced.
I thought it was stupid to let the air slow down in that
five-inch pipe and then try to speed it up again out of
a smaller diameter nozzle. I have the same thrust with this
nozzle as with the old one, but the turbine temperature
was much lower.

Extended jet nozzle
This is the jet
nozzle that I am now using Even with the extreme heat the
turbine is in good condition. The nozzle has been extended
in length from the previous version shown above.
I have worked
a year on this engine and the best thrust output that I
managed was 45 pounds of thrust. This is the engine that
was used on the jet kart. I tried different nozzle sizes
and even used a jet nozzle that was the same diameter of
the turbine. The fuel consumption is 13 gallons an hour.
The problem that I have run into is the higher thrust levels
caused severe overheating of the turbine. The turbine inlet
temperature climbs to over 1900 degrees Fahrenheit with
a turbine outlet temperature of 1700 degrees. I only kept
the output high for a few seconds at a time. I have tried
to lower the temps but all attempts have failed. It seems
that every time it ran cooler the thrust output was considerably
lower.
These tests were
conducted using the same fuel pressures and nozzle sizes.
All of the tests have led me to the conclusion that the
combustor is too small. The air flow through the combustor
is too high and the fuel is taking to long to fully burn
and is entering the turbine scroll while it is still burning.
I have started work on a new combustor, flame tube and inlet
pipe. It will also use two smaller fuel nozzles to try to
control the burn time. I do not know if this will perform
any better, but I will try nonetheless. I have not totally
given up on this design yet. I am reconfiguring the combustion
chamber so that the air will now come in on the side closer
to the top. This should swirl the air around in the combustor
more and help in the combustion of the fuel. I am also going
to change the fuel injector nozzles to attempt to get better
atomization.
.

New fuel nozzles
I purchased several
water misting nozzles from Mc Master Carr. I will test them
first and see if they will deliver smaller fuel droplets.
If so, I think it should complete the burn by the time it
reaches the secondary air holes. Testing will verify if
this is the case or not.

The new nozzle installed on the combustor
Sept 28, 2005
I tested the new nozzles I received from Mc Master Carr
and found that they do deliver a finer mist compared to
the agricultural nozzles that I had been using. I will be
finishing up the modifications and will test the engine
soon.

Nozzle mounted to end cap
The new nozzles
mount to the combustor end cap in the same way as the previous
agricultural nozzles. The smaller tube to the left of the
nozzle is the propane inlet, which serves as the pilot to
ignite the diesel fuel as it is injected into the combustor
through the main nozzle.

Relocated air inlet
The air inlet
to the combustor was relocated to create a better air distribution
throughout the entire length of the flame tube.

Combustor sealed
As the air inlet
to the combustor was relocated, the original inlet hole
had to be sealed. A piece of plate steel was formed to match
the outer radius of the combustor and was welded in place
over the old opening.

Top of flame tube
There is a small
opening at the top of the flame tube to cut down on the
amount of air that is getting by. The fuel is sprayed directly
into the hole on the end of the flame tube.
As of Sept 30,
2005 I had finished work on the modified combustor and tried
to start it. A let down to say the least. I was almost able
to get it to spool up, but it would flame out. I think that
there was too much frontal air getting around the nozzle.
There are air holes along the side of the nozzle, and with
the relocation of the air inlet it would appear that there
was too much airflow that was interfering with the burn
process directly after the nozzle. It was time to redesign
the flame tube at the nozzle and inlet areas and retry.
With further
modifications and testing completed, I reassembled the engine
and was able to start it. It ran well and the temps were
down. Sealing off the top of the flame tube worked well.
The turbine inlet temp was 1200 degrees Fahrenheit instead
of 1700 to 1900 and the turbine outlet temp was at 1000
degrees. The thrust was not quite as good as I wanted, as
it was only 38 pounds at full throttle. I am using a 15
gph (gallon per hour) nozzle, but with a much finer spray.
The next thing I checked for were any cold spots in the
flame tube where the fuel was not burning correctly. The
maximum combustor pressure reached was 32 PSI. The combustor
needed to reach an internal pressure of 40 PSI to see any
noticeable increase in thrust output over the previous results.
It would appear that the combustor was consuming more fuel
without a noticeable increase in power output.
Additional work
on the engine yielded acceptable results. I was able to
get the thrust back up and it was atomizing and burning
the fuel well. The temperatures will still go very high
on the TIT's (turbine inlet temperature) but the TOT's (turbine
outlet temperature) are marginally safe. I took the engine
for a drive (see the jet kart for the details). The engine
did not reach the 40 PSI combustor pressure but did manage
to get up to 36 PSI. I added an improved nozzle to the jet
pipe and it seems to have helped.
With this stage
of engine development and testing complete, the engine was
grafted onto a go cart chassis. Full details of the jet
kart and the build are available in the jet
kart section of the site. The engine has since undergone
a new development stage which is documented in the HR-1A
section of the site. It is the further development of the
engine with a new combustion chamber designed to achieve
maximum power from the engine.
I hope that you
have enjoyed reading about the initial development of the
HR1 engine.
Gary Richards
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